Today's instalment is called: A Quest for Perfection.... or Ron's Neurotic Obsession.
The new EP-2 runs very well overall. But one of the Cabs in particular just.... somehow I knew it could be better.
My guess was the inner bearing.
I really don't like some aspects of the design KMT gave me.
One is that I would have preferred the motor shaft to be really long and have an OUTBOARD bearing that was held tightly (no wiggle).
This short shaft business simply does not seem optimal.
So I decided to remove the inner bearing and find a way to support the motor at exactly the correct height.
Another reason to walk though this is that it shows how effective building the modular wiring harness is. In what follows, know that I disassembled and assembled this loco probably about a dozen times as I made experimental tweaks.
So here is the Cab. Remove the three screws to the shell and lay the shell to the side-- watching those LED wires. I don't want to pull them or scratch the coating off.
Pull the decoder plug.
Pull the red boiler room jumper wire.
The shell is now free.
Pull the wire from the front truck pad.
Remove the power truck and the gearbox.
Lift the heatsink off the motor. (this is actually my frame connection.)
Remove the two screws to the motor.
Pull the motor assembly free.
Now the idea here is that I need some kind of shim to go under the motor.
Here is my calliper and a LOT of experimentation.
80 mil was too big. 40 + 10 was too small. 60 mil was close.
After a LOT of experimentation and searching, I found I had some fat two-sides perfboard.
I cut a piece off.
Ok, let's measure this.
Into the calliper.
As you can see, it measure a little over 64 mil. I'll add something to this.
Cut a triangular piece.
Trim the sharp tips.
This size is good for support under the motor while not covering the hole for the red wire.
Superglue. Getting just a little on the tip.
Add glue around the base.
Pieces of paper range from about 3 mil to 4 mil. here I am adding a piece of 4 mil.
Superglueing it down.
So now, I am right about at 68 mil.
Now to remove the inner bearing. USed a NWSL gear puller.
Install the motor.
Here you can see the shim.
Reassemble to test in analog mode.
test run shows that this worked. Just right.
Reassemble with decoders. Reset the decoder to be sure and start from scratch.
Run both Cabs to see the speed matching.
in this case, the A cab ran faster. So the B unit was my reference.
I programmed the B Cab to run a a good top speed.
Then with experimentation, I programmed the A Cab to match.
This was just a rough estimate using the Vstart, Vmax, and Vmid variables.
Experimentation (and recordkeeping!) allowed me to get them very close.
It worked! Both decoders are programmed to #3 and the loco is run as one. But the speed matching of the decoders is just what this pair needed for maximum efficiency.